Yesterday, Bill, the owner made the command decision to continue the boat delivery trip. The canal authority managed to dredge the Fish Creek location and was moving their equipment to Wood Creek on Friday where the depths were in the neighborhood of seven feet. They said that if we got hung up their tugs would be on station doing dredging and could drag us through.
Leaving Erie a bit after 1600 with a slight change in crew (Bill”s brother Bob replacing Rick), we arrived at the boat in Rome at 2230 hours and were pleased to find that the homeless had cleaned up after themselves and left the boat exactly as they found it (and we left it). Actually, the only evidence that anybody had been around the boat was a fishing lure and a hook that was embedded in the stern line.
I am surprised that the owner of this lure didn’t come aboard to retrieve his fishing gear.
The new canal facilities promised to us a few years ago by the former mayor of Rome finally appeared this trip. They have very nice bathroom/shower facilities across the street from the docks. Unfortunately the facilities only appear to be open during normal business hours which didn’t do us any good in the evening or early morning.
Rome’s very nice restroom facility on the canal.
A beautiful day in Rome with few boats on the wall.
The first order of business in the early morning was to grab some breakfast at a local greasy spoon and then a stop at the grocery store for some essentials. Bill the had to return the rental car to the airport after which we fired up the engine and got under way at 0930. Lock 21 awaited us about an hours motor from Rome. This lock would drop us about twenty five feet down, one of only two looks that would lower us on this trip. The rest of the locks would raise us. Two other boats joined us in the lock, both of them taking the port side wall while we positioned ourselves on the starboard side wall. Even though we were first in to the lock we told the first port side boat (Mainship Trawler) to leave first. As he left one of the lock lines either got tangled in one of his stern cleats, or was somehow still attached. The boat went forward and rolled heavily to one side as the line lifted his stern. This line, stretched to it’s limit and about 30′ long ripped the cleat from his stern and the line catapulted over the top of the lock. It was pretty impressive to see although the owner of the boat wasn’t terribly happy about the situation.
In lock 21 before they sent us down 25′ and the Mainship on our port side lost their stern cleat.
Once clear of Lock 21 we entered Lock 22 about a half mile away and locked through with out incident. As we exited we let the trawler that was astern of us pass as the dreaded Woods Creek shoal was just around the bend from the lock. We didn’t want to hold anybody up if (when) we ran aground. Sure enough, we stuck the keel into the bottom as expected. The dredge crew was sitting not far from where we hit and we backed off and asked for advice. They told us the actual shoal was only about five feet wide and to move a little closer to shore and try again. Raising the keel a few inches and attacking the shoal with some boat speed we slowed but then bulled our way though. It turned out this was either loose sand or mud. There was none of the horrific grinding noise we had heard when we pushed the keel and rudder through gravel a few weeks ago. We were once more on our way. What was interesting was that coming out of Lock 22 our depth finder ceased to function, it was locked on to 15.3 feet. As we were busy trying to pick a path across the shoal we didn’t have time to fuss with it and since it wasn’t working we weren’t distracted by it as the depth quickly decreased under us. After getting by the shoal we re-booted the electronics and the depth finder came back to life.
We provided a little entertainment for the guys working the dredge at Woods Creek.
We ran into some skinny water in the channel into Lake Oneida (roughly nine feet) but once into the lake made the 20 mile run up into Brewerton where we took on 16 gallons of fuel, pumped out the holding tanks and filled the fresh water tanks. The ride across the lake was great as we had a light rail wind. That beats the normal bashing we seem to get in Liberty.
At the dock was the a Fisher 30 motor sailor, Celtic Cross. We had read of her “exploits” on Lake Erie from the blog of the LNVT Nellie D. To make a long story short, the owner of Celtic Cross had purchased the boat on the upper lakes and was heading home to Virginia, single handing the boat. Evidently he ran into a storm on Lake Erie a few weeks back and after spending two plus days straight at the wheel was taken in tow by the Canadian Coast Guard after being blown off course by fifty miles. He ended up in the hospital for a few days before continuing. I went over to introduce myself to him and he said that he tried to cross Lake Oneida this morning but hadn’t gotten too far before the transmission failed. Evidently the case is cracked and who knows what else needs replaced. It will take a month or so to get parts and get it fixed so he is jumping on a plane and heading back to Virginia. He has put the boat up for sale and depending on how he feels or if it sells he will make a decision at a later time on how to proceed.
Mike’s Fisher 30. We have always been partial to boats that are pointy on both ends, this being the stern view of the boat.
At the dock in Brewerton.
Bill installed the new “penguin” control for the AC unit that was supposed to make it operational. It did, to a point. The unit would heat but not cool. After a few phone calls it was determined that a secondary sensor on the AC unit itself was not compatible with the new control. The fix was to simply cut the wires to the secondary sensor and let the primary sensor on the control unit do it’s thing. At that point the cooling function came to life and now all is good.
The new AC controller. As you can see by the temperature it is a good thing this became functional.
The Brewerton Boat Yard works on some pretty big boats and they have a pretty big fork lift.
After a nice walleye dinner at a local watering hole along the canal we retired to the boat where the owner busied himself with scrubbing the topsides while sipping an adult beverige while the rest of the crew sat in the cockpit and visited with Mike, the almost ship wrecked sailor.
A ten minute walk got us to the Waterfront Tavern which overlooks the canal (entry/exit to Lake Oneida).
Today, 31.4 nm in 5-1/2 hours. Total for the trip: 503 nm. We need to pick up the pace.
Dave